API: 15-081-21286
Operator: Chesapeake Operating, LLC Field: Eubank South Lease: MLP Rooney Well 4-5 |
Location: T30S R34W, Sec. 5, SW NW NE
4054 North, 2095 West, from SE corner Longitude: -101.0599478 Latitude: 37.4715553 County: Haskell Status: OIL-P&A |
Spud Date: 06-MAR-00
Completion Date: 17-APR-00 Plugging Date: 23-MAY-07 Total Depth: 5700 Form. at depth: MISSISSIPPIAN Elevation: 3010 KB |
Test Number: 1 | Data Source: TRILOBITE |
Interval: 5245 to 5322
Formation tested: Upper Morrow | Date, Time: 13-MAR-00; 14:38:27 |
Initial Hydro Pressure: 2538 PSI
First Initial Flow Pressure: 81 PSI First Final Flow Pressure: 161 PSI Initial Shut-in Pressure: 990 PSI Second Initial Flow Pressure: 160 PSI Second Final Flow Pressure: 231 PSI Final Shut-in Pressure: 920 PSI Final Hydro Pressure: 2449 PSI |
Tool Data Hole Size: 8.875 in. Drill Collar ID: 2.25 in. Drill Pipe ID: 3.8 in. Drill Collar Length: 245 ft. Drill Pipe Length: 4747 ft. |
Initial Flow: Fair to strong blow off bottom in 2 minutes. Initia Shut-In: Weak 1/4"" return died at 35 minutes. Final Flow: Fair to strong blow off bottom in 2 minutes. Gas to surface in 40 minutes. Too small to measure. Final Shut-In: Weak 1/2"" return died at 60 minutes. |
|
Bottom Hole Temperature: 124 DEG F
Percent Porosity: Samples: Gas Recovery: Comments: | |
Recovery 575 of Total Fluid 245 of Fluid in Drill Collars 330 of Fluid in Drill Pipe 75 of Slightly gas cut mud 500 of Frothy gassy oil 35 of Gravity (API) | |
View Pressures | No Recovery Gas data. |
Download original data
ZIP file contains the orignal DST data supplied to the KGS by Trilobite Testing LLC . Four files are in each archive. The .flg file is an ascii file that has time and pressure at change points (open, shutin, etc.). The .csv is the original data extracted into a comma delimited file. The last two files (the .inf file and a file with a variable extension) are binary files that require Alpine DST software for display. | |