API: 15-119-21024
Operator: Hartman Oil Co., Inc. Field: Borchers Northwest Lease: Calhoon 'A' Well 1 |
Location: T33S R29W, Sec. 11, SE NW NE NE
626 South, 984 West, from NE corner Longitude: -100.4378596 Latitude: 37.1964936 County: Meade Status: D&A |
Spud Date: 25-MAY-00
Completion Date: 06-JUN-00 Plugging Date: 07-JUN-00 Total Depth: 5676 Form. at depth: CHESTER Elevation: 2553 KB |
Test Number: 1 | Data Source: TRILOBITE |
Interval: 5607 to 5657
Formation tested: Morrow | Date, Time: 05-JUN-00; 14:43:05 |
Initial Hydro Pressure: 2707 PSI
First Initial Flow Pressure: 62 PSI First Final Flow Pressure: 95 PSI Initial Shut-in Pressure: 233 PSI Second Initial Flow Pressure: 94 PSI Second Final Flow Pressure: 113 PSI Final Shut-in Pressure: 253 PSI Final Hydro Pressure: 2680 PSI |
Tool Data Hole Size: 7.78 in. Drill Collar ID: 2.25 in. Drill Pipe ID: 3.8 in. Drill Collar Length: 304 ft. Drill Pipe Length: 5284 ft. |
Initial Flow: Weak 1/2"" built to strong bottom of bucket in 20 minutes. Initial Shut-In: No blow back. Final Flow: Weak 1/2"" built to strong bottom of bucket in 12 minutes. Final Shut-In: No blow back. Remarks: Est. 14 Ft. of Pay. |
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Bottom Hole Temperature: 125 DEG F
Percent Porosity: 15 Samples: None Gas Recovery: Comments: | |
Recovery 200 of Total Fluid 200 of Fluid in Drill Collars 720 of Gas in pipe 140 of Slightly gas cut mud 60 of Oil & gas cut mud | |
View Pressures | No Recovery Gas data. |
Download original data
ZIP file contains the orignal DST data supplied to the KGS by Trilobite Testing LLC . Four files are in each archive. The .flg file is an ascii file that has time and pressure at change points (open, shutin, etc.). The .csv is the original data extracted into a comma delimited file. The last two files (the .inf file and a file with a variable extension) are binary files that require Alpine DST software for display. | |