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Specific Well--15-129-20983

Yearly Pressure Data

API: 15-129-20983
Operator: Anadarko Petroleum Corp.
Field: Hugoton Gas Area
Lease: MINGENBACK 'C'
Well 1-A
Location: T33S R40W, Sec. 28, NW SE SE
1050 North, 1100 West, from SE corner
Longitude: -101.6678349
Latitude: 37.144591
County: Morton
Status: GAS
Spud Date: 29-APR-89
Completion Date: 13-MAY-89
Plugging Date:
Total Depth: 6150
Form. at depth: MISSISSIPPIAN
Elevation: 3325 KB
From KCC: 15-129-20983-00-00: Mingenback 'C' 1A - Intent and ACO-1 were both filed with the KCC. The rig was skidded after the drill pipe got stuck and the hole was lost on 15-129-20979-00-00. This was a gas well completed 05/13/1989 as dry hole. Set Surface and Production Casing but found to be unproductive deep at 6150. Thoughts were to recomplete as Hugoton infill well. MCM 2 Jul 2008
Year Acreage Shut-In
Pressure
Working
Pressure
Daily Rate Open Flow Adj.
Deliverability
Water
Production
Meter
Pressure
Differential Coefficient Dry Gas
Gravity
1996 640 66.9 56.1 175.21 558 455 0 55.4 12.84 5852.7  
1997 640 0 0 0 0 455 0 0 0 0  
1998 640 36.3 27.5 91.72 227 206 0 27.3 5.89 5852.7  
1999 640 0 0 0 0 206 0 0 0 0  
2000 640 23.4 6.1 111.75 132 132 0 5.2 18.6 5852.7  
2002 640 0 0 0 0 0 0  
2003 640 0 0 0 0 0 0  
2004 640 0 0 0 0 0 0  

Kansas Geological Survey, Gas Proation Database
Comments to webadmin@kgs.ku.edu
URL=http://www.kgs.ku.edu/Magellan/Proration/index.html
Programs Updated June 4, 2002. Data added periodically.