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Specific Well--15-129-20983Yearly Pressure Data |
API: 15-129-20983
Operator: Anadarko Petroleum Corp. Field: Hugoton Gas Area Lease: MINGENBACK 'C' Well 1-A |
Location: T33S R40W, Sec. 28, NW SE SE
1050 North, 1100 West, from SE corner Longitude: -101.6678349 Latitude: 37.144591 County: Morton Status: GAS |
Spud Date: 29-APR-89
Completion Date: 13-MAY-89 Plugging Date: Total Depth: 6150 Form. at depth: MISSISSIPPIAN Elevation: 3325 KB |
From KCC: 15-129-20983-00-00: Mingenback 'C' 1A - Intent and ACO-1 were both filed with the KCC. The rig was skidded after the drill pipe got stuck and the hole was lost on 15-129-20979-00-00. This was a gas well completed 05/13/1989 as dry hole. Set Surface and Production Casing but found to be unproductive deep at 6150. Thoughts were to recomplete as Hugoton infill well. MCM 2 Jul 2008 |
Year | Acreage | Shut-In Pressure |
Working Pressure |
Daily Rate | Open Flow | Adj. Deliverability |
Water Production |
Meter Pressure |
Differential | Coefficient | Dry Gas Gravity |
---|---|---|---|---|---|---|---|---|---|---|---|
1996 | 640 | 66.9 | 56.1 | 175.21 | 558 | 455 | 0 | 55.4 | 12.84 | 5852.7 | |
1997 | 640 | 0 | 0 | 0 | 0 | 455 | 0 | 0 | 0 | 0 | |
1998 | 640 | 36.3 | 27.5 | 91.72 | 227 | 206 | 0 | 27.3 | 5.89 | 5852.7 | |
1999 | 640 | 0 | 0 | 0 | 0 | 206 | 0 | 0 | 0 | 0 | |
2000 | 640 | 23.4 | 6.1 | 111.75 | 132 | 132 | 0 | 5.2 | 18.6 | 5852.7 | |
2002 | 640 | 0 | 0 | 0 | 0 | 0 | 0 | ||||
2003 | 640 | 0 | 0 | 0 | 0 | 0 | 0 | ||||
2004 | 640 | 0 | 0 | 0 | 0 | 0 | 0 |