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API: 15-057-20883-0001
KID: 1044635999
Lease: Ford Co L&C Co
Well: 1-16
Original operator: Vincent Oil Corp.
Current operator: Vincent Oil Corporation
Field: Wildcat
Location: T29S R24W, Sec. 16
SW NE NE NW
4899 North, 3246 West, from SE corner
NAD27 Longitude: -99.9536158
NAD27 Latitude: 37.5292974
NAD83 Longitude: -99.95403
NAD83 Latitude: 37.52932
Lat-long from GPS
County: Ford
Permit Date: Oct-25-2013
Spud Date: Nov-04-2013
Completion Date: Jan-07-2014
Plugging Date:
Well Type: GAS
Status: Producing
Total Depth: 6150
Elevation: 2549 KB
Producing Formation: Viola
IP Oil (bbl):
IP Water (bbl):
IP GAS (MCF):
KDOR code for Oil: 148572
KDOR code for Gas: 233958
KCC Permit No.:
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Drill Stem Tests Taken: No
Samples Set to Survey: Yes
Cores Taken: No
Electric Logs Run: Yes
Sonic
Method of Completion:
Date of First or Resumed
Production/Injection:
Producing Method:
Estimated production per 24 hours
    Oil:
    Water:
    Gas:
Disposition of Gas:
Tubing record
    Size: 2.3750
    Set at: 5230
    Packer at:
Production intervals:

Casing record

new or used? New
Purpose of String Size Hole
Drilled
Size Casing
Set (in O.D.)
Weight
Lbs/Ft
Setting
Depth
Type of
Cement
# Sacks
Used
Type and Percent
Additives
Surface Casing 12.25 8.625 23 646 65 /35 POZ & Common 320 2-6% Gel, 3% CC & 1/4# Flo-seal/sx
Production Casing 7.875 4.5 11.6 5385 Pro C 175 5#/sx Gilsonite

Additional Cementing/Squeeze Record

purpose?
Depth
Top Bottom
Type of Cement # Sacks Used Type and Percent Additives

Perforation Record

Shots Per Foot Perforation record Material Record Depth
4 5206' to 5218' Perf: 5206' to 5218', ran 2 3/8" tubing to 5220', SDFN;
Acidized with 1500 gal 15% MCA, ran addition joint of tubing, set at 5230';
Swabbed 5 hrs, final rate 9 bbl/hr (0% Oil), KOF good gas blow; SDFN; SICP 1200#, SITP 1000#,
Flowed for 3hrs with deceasing fluid and increasing gas blow,
rigged down, set temp gas pac, tested 156 MCFG, shut in ,
waiting on pipeline connection


Kansas Geological Survey, Oil and Gas Well Database
Comments to webadmin@kgs.ku.edu
URL=http://www.kgs.ku.edu/Magellan/Qualified/index.html
Data added continuously.