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API: 15-009-26023-0002
KID: 1046798302
Lease: KUFELD
Well: 1-19
Original operator: F. G. Holl Company L.L.C.
Current operator: F. G. Holl Company L.L.C.
Field: Heizer Southwest
Location: T19S R14W, Sec. 19
N2 SW SW
1000 North, 700 East, from SW corner
NAD27 Longitude: -98.9194823
NAD27 Latitude: 38.3790493
NAD83 Longitude: -98.919852
NAD83 Latitude: 38.379062
Lat-long calculated from footages
County: Barton
Permit Date:
Spud Date: Aug-31-2015
Completion Date: Sep-25-2015
Plugging Date:
Well Type: OIL
Status: Recompleted
Total Depth: 3770
Elevation: 1915 KB
Producing Formation: Arbuckle
IP Oil (bbl):
IP Water (bbl):
IP GAS (MCF):
KDOR code for Oil: 145659
KCC Permit No.:
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Drill Stem Tests Taken: No
Samples Set to Survey: No
Cores Taken: No
Electric Logs Run: No
Method of Completion: Perforated
Date of First or Resumed
Production/Injection: Sep. 25, 2015
Producing Method: tried to pump but not good well
Estimated production per 24 hours
    Oil:
    Water:
    Gas:
Disposition of Gas:
Tubing record
    Size: 2.8750
    Set at: 3625
    Packer at:
Production intervals: 3244 ; 3560

Casing record

new or used? New
Purpose of String Size Hole
Drilled
Size Casing
Set (in O.D.)
Weight
Lbs/Ft
Setting
Depth
Type of
Cement
# Sacks
Used
Type and Percent
Additives
Surface 12.25 8.625 28 850 A-Con & Common 400 0
Production 7.875 5.5 14 3766 AA-2 & Scavenger 150 0

Additional Cementing/Squeeze Record

purpose? Plug Off Zone
Depth
Top Bottom
Type of Cement # Sacks Used Type and Percent Additives
3553 to 3567 common 50
3244 to 3417 60/40 poz 150

Perforation Record

Shots Per Foot Perforation
Top
Perforation
Bottom
Bridge Plug
Type
Bridge Plug
Set At
Material Record
4 3551 3560 Spotted 150 gal 15% MOD 202 acid. 250 gal 15% MOD 202 acid
3414 3417 Squeezed old Arbuckle perfs: 3553' - 3567'
3271 3274 50 gal 15% nefe acid
3283 3288 Squeezed all LKC perfs: 3244' - 3417'
3244 3248
4 3244 3248 Spotted 250 gal 15% NEFE acid
4 3271 3274 Spotted 250 gal 15% NEFE acid
4 3277 3281 Spotted 500 gal 15% NEFE acid
Spotted 250 gal 15% DSFE acid

Information from Outside Sources

Please note: The link below takes you away from the web site of the Kansas Geological Survey to the website of the Kansas Geological Society, a library in Wichita. The Survey can not help with information presented by the Walters Digital Library.

From Kansas Geological Society's Walters Digital Library


Kansas Geological Survey, Oil and Gas Well Database
Comments to webadmin@kgs.ku.edu
URL=http://www.kgs.ku.edu/Magellan/Qualified/index.html
Data added continuously.