Specific Well--15-095-22344
Engineering Data | ||
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API: 15-095-22344
KID: 1052097295 Lease: MALONEY Well: 2-15 Original operator: Vincent Oil Corporation Current operator: Vincent Oil Corporation Field: Location: T28S R8W, Sec. 15 N2 SE SE SE 420 North, 330 West, from SE corner NAD27 Longitude: -98.1730454 NAD27 Latitude: 37.6047934 NAD83 Longitude: -98.1733886 NAD83 Latitude: 37.6048101 Lat-long calculated from footages |
County: Kingman
Permit Date: Nov-17-2021 Spud Date: Dec-08-2021 Completion Date: Feb-09-2022 Plugging Date: May-10-2024 Well Type: GAS-P&A Status: Plugged and Abandoned Total Depth: 4105 Elevation: 1596 KB Producing Formation: IP Oil (bbl): IP Water (bbl): IP GAS (MCF): KCC Permit No.: |
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Drill Stem Tests Taken: Yes Samples Set to Survey: Yes Cores Taken: No Electric Logs Run: Yes Attached Method of Completion: Perforated Date of First or Resumed Production/Injection: |
Producing Method: Estimated production per 24 hours Oil: Water: Gas: Disposition of Gas: Tubing record Size: Set at: Packer at: Production intervals: 4028 ; 4036 |
Casing recordnew or used? New |
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Purpose of String | Size Hole Drilled |
Size Casing Set (in O.D.) |
Weight Lbs/Ft |
Setting Depth |
Type of Cement |
# Sacks Used |
Type and Percent Additives |
---|---|---|---|---|---|---|---|
Surface | 12.25 | 8.625 | 23 | 293 | 60/40 POZ | 275 | 2% Gel, 3% CC & 1/4# Cel Flake/sx |
Production | 7.875 | 4.5 | 11.6 | 4287 | Pro-C | 150 | 2% Gel & 10% Salt |
Additional Cementing/Squeeze Recordpurpose? Plug Off Zone |
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Depth Top Bottom |
Type of Cement | # Sacks Used | Type and Percent Additives | ||||
---|---|---|---|---|---|---|---|
4028 to 4035 | Common | 200 | Last 75 sx 2% chloride |
Perforation Record |
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Shots Per Foot | Perforation Top |
Perforation Bottom |
Bridge Plug Type |
Bridge Plug Set At |
Material Record | ||
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4 | 4028 | 4035 | Perf 4028-4035, Ran tubing to 4036, SDFN. | ||||
Acidized with 750 gal 15% MCA, RU to Swab, Swab 5hrs , rec 129 bbls Wtr, FL at 2300', SDFN | |||||||
TP 70#, CP 400#, FL at 1450', Ran in with packer to test BTM plug | |||||||
Set Packer at 4068',4100', 4133', 4165' 4198', & 4245'. pressured up to 1000#. Bled off to 700#. | |||||||
CIBP Cast Iron Bridge Plug | 4228 | Btm plug leaking, pulled tubing & packer, SDFN. RU Wireline & set CIBP at 4228 & capped with 2 sx Cmt., Ran tubing , SDFN | |||||
TP 0#, CP 0# FL at 1600', RU to swab, swab for 2 hrs, rec 66 bbl wtr, FL at 2300', pressured tubing to 1000# & held, SDFN | |||||||
RU Tubing & packer to test Btm plug and csg above perfs. Set packer at 4041' & pressured up to 1000#. Btm plug leaking. | |||||||
Set packer above perfs at 4020 & pressured up to 1000# & pressure held. SDFN (Will SQZ Btm plug & perfs) | |||||||
Set packer at 3946' & Sqz'd btm plug & perfs with 200 sx common. Released packer & pulled out | |||||||
Determined that packer slips were lost in wellbore while tripping out with tubing & packer. Will WOC for 10 days . | |||||||
Re-entered casing and fished for packer slips, then milled and drilled on cmt for 3-4days .to clear wellbore of slips and cmt. | |||||||
Ran in with wireline and re-perf 4028' to 4035 (4SPF). Ran in with tubing, MA & SN and set tubing at 4036. Acidized with 500 gal 15% MCA' | |||||||
RU to Swab, swab 2 hrs & rec 36 bbls wtr.. SDFN SITP 5# SICP on vac, FL at 1800'. Swab 3hrs & rec 71 bbls wtr with FL at 2300'. No gas kick after swab runs. | |||||||
Pulled tubing and shut in well. Will TA well to evaluate shallow gas potential or Plug and Abandon. |
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From Kansas Geological Society's Walters Digital Library