Specific Well--15-129-20983
General Well Data | ||
API: 15-129-20983
KID: 1006096076 Lease: MINGENBACK 'C' Well: 1-A Original operator: Anadarko Petroleum Corp. Current operator: Anadarko Petroleum Corporation Field: Hugoton Gas Area Location: T33S R40W, Sec. 28 NW SE SE 1050 North, 1100 West, from SE corner NAD27 Longitude: -101.6678349 NAD27 Latitude: 37.144591 NAD83 Longitude: -101.6682748 NAD83 Latitude: 37.1446157 Lat-long calculated from footages |
County: Morton
Permit Date: Spud Date: Apr-29-1989 Completion Date: May-13-1989 Plugging Date: Well Type: GAS Status: Recompleted Total Depth: 6150 Elevation: 3325 KB Producing Formation: Chase Group IP Oil (bbl): IP Water (bbl): IP GAS (MCF): KDOR code for Gas: 217211 KCC Permit No.: |
From KCC: 15-129-20983-00-00: Mingenback 'C' 1A - Intent and ACO-1 were both filed with the KCC. The rig was skidded after the drill pipe got stuck and the hole was lost on 15-129-20979-00-00. This was a gas well completed 05/13/1989 as dry hole. Set Surface and Production Casing but found to be unproductive deep at 6150. Thoughts were to recomplete as Hugoton infill well. MCM 2 Jul 2008 | |
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ACO-1 and Driller's Logs
Wireline Log Header Data
Tops Data
Gas Production DataThis well has been linked to a gas lease. Proration Gas Pressure Tests
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Information from Outside SourcesPlease note: The link below takes you away from the web site of the Kansas Geological Survey to the website of the Kansas Geological Society, a library in Wichita. The Survey can not help with information presented by the Walters Digital Library. |